Home » Ex-USAF F-4 pilot tells how he managed to land his Phantom II safely following the right engine explosion

Ex-USAF F-4 pilot tells how he managed to land his Phantom II safely following the right engine explosion

by Till Daisd
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F-4E-Landing

The fuel flow controller on the F-4 Phantom II had NEVER broken down. It wasn’t mentioned in the flight handbook, the book of emergency procedures, or anywhere else

The McDonnell two-place, twinjet, all-weather F-4 Phantom II, with top speeds exceeding the speed of sound, had its first flight in May 1958 and was initially designed for US Navy fleet defense. It entered service in 1961 and was one of the most versatile fighters ever constructed.

More Western air forces used it than any other plane in the first line. In addition, the F-4 served as the main fighter-bomber for the US Air Force (USAF) in the 1960s and 1970s, and it was still used in the “Wild Weasel” anti-aircraft missile suppression role in the mid-1990s.

‘The F-4 Phantom’s fuel flow controller had NEVER malfunctioned. It wasn’t listed in the book of emergency procedures, the flight manual, or anywhere,’ Charlie Noak, former F-4 Phantom II pilot with the US Air Force, recalls on Quora.

‘Hot August day, 1987. As number three in a flight, I was at full power to join up, coming closer, I started to pull the power back. Then, the full flow control failed to the free flow condition. Before I could pull the right throttle back to shut off the engine, The exhaust gas temperature had climbed above 1,570 degrees, the engine was spinning at 114%. The total time for the right engine to explode was less than three seconds. Huge fireballs out the front and back. Cut through the engine casing, and cut a hydraulic line. Now I had a recognizable emergency; engine out with loss of utility hydraulic system failure coming on steadily. Never turn into a bad engine. I was able to maneuver back to the runway, staying away from all habitations, and head down finally. The hydraulic system completely failed on short, too low to bail out. I landed, straight, fortunately. No drag chute deployment, no brakes, no steering, etc. Fortunately, the runway was 8,000′ long, uphill, and directly into the wind. After the explosion, there was no fire, that was blown out.

‘We came to a stop just even with the de-arm area, The fire truck gave us a nice foamy shower, then towed us clear of the runway. Once the canopies had been manually opened, I dropped my oxygen mask. The humid smell of growing corn had never smelled so sweet.’

Noak concludes;

‘Earlier, I had given my encouragement for my Weapons Systems Officer (WSO) to eject.

‘“What are you going to do, Charlie.”

‘“I have to go land this piece of s**t so we can figure what went wrong, and possibly fix the fleet.”

‘“Okay, I’ll do that too.”

Oh dear God look after this naive fool, he has a good heart.

‘“(Are) you coming?”

‘“Oh, I’ll be along in a few minutes, give me time to pull the seat cushion out of my a*s.”’

Photo by: U.S. Air Force / NARA

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